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Front Engine Dragsters / Finally down the track on second outing..
« on: November 12, 2019, 09:33:28 AM »
Finally got the MW car together and down the track semi-successfully on our second outing.
Been 12 months of assembly, other projects and work.
First time to track since took the car down all seemed fine, burnout was uneventful and I decided to do a footbrake leave in high gear just to see if it went straight and stopped well. Didn't worry about cutting a light and had asked for a single lane run since we were shaking the car down. Car spun just a bit but left straight - felt really good until about the 330 when I got a visor / face load of nice warm oil and backed her down quick - blazing trap speed of 59 MPH. Note to self - put visor ALL the way down every time.
Turns out that the three piece Enderle injection manifold / intake gaskets / china rail interfaces needed some minor machine work and some additional Ultra Grey. Acceleration was pushing oil back into the valley / head corners that found a direct leak path into my helmet.
Second time to track I can report a better outcome. 6 passes, all but one was high gear roll into the throttle leave as we continue shaking down. Best was 5.80 @ 132. The single TB pass was an absolute comedy.....I think I remember three distinct wheelies during the pedal party.
I've got to get the go-pro rigged up in the cockpit to keep an eye on the tach - was spinning a bit around the 100' mark and quite a bit near the finish line. Top end spin I'm thinking is around the point it's coming up on the high speed. Kept going down in tire pressure ended up at 7 lbs. Friend that was helping me out commented the tires seemed pretty stiff - we checked with a variety of gauges in the pits and turns out my low pressure gauge is fubar - 7=11. Our day was over but a new gauge is on the way.
Reasonable tire pressure test session coming soon....
Been 12 months of assembly, other projects and work.
First time to track since took the car down all seemed fine, burnout was uneventful and I decided to do a footbrake leave in high gear just to see if it went straight and stopped well. Didn't worry about cutting a light and had asked for a single lane run since we were shaking the car down. Car spun just a bit but left straight - felt really good until about the 330 when I got a visor / face load of nice warm oil and backed her down quick - blazing trap speed of 59 MPH. Note to self - put visor ALL the way down every time.
Turns out that the three piece Enderle injection manifold / intake gaskets / china rail interfaces needed some minor machine work and some additional Ultra Grey. Acceleration was pushing oil back into the valley / head corners that found a direct leak path into my helmet.
Second time to track I can report a better outcome. 6 passes, all but one was high gear roll into the throttle leave as we continue shaking down. Best was 5.80 @ 132. The single TB pass was an absolute comedy.....I think I remember three distinct wheelies during the pedal party.
I've got to get the go-pro rigged up in the cockpit to keep an eye on the tach - was spinning a bit around the 100' mark and quite a bit near the finish line. Top end spin I'm thinking is around the point it's coming up on the high speed. Kept going down in tire pressure ended up at 7 lbs. Friend that was helping me out commented the tires seemed pretty stiff - we checked with a variety of gauges in the pits and turns out my low pressure gauge is fubar - 7=11. Our day was over but a new gauge is on the way.
Reasonable tire pressure test session coming soon....