Arrived at NDRL race in Bowling Green yesterday.
Wired up the flapper I n the tank and made 4 time trials.
The problem is not completely fixed but better.
We have been trying to run an 8.5 index all summer.
Decided that as this is the last race of the season to push it a little harder.
first pass was 8.371, second was 8.129,
third we leaded it out and pushed more air had a .040 r/t on the .400 pro tree and ran 8.035 and on the fourth pass had a reaction time of .037 and ran 8.093 on the same tune and the a/d had gone away by 200 feet. I think we are in the ball park, but still the fuel pressure drops a little off the line?
??