Technical > Matt Shaff's Engine Shop

sorry need help again

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hotrod316:
just primed the motor for 30 mins.  waited 30 mins removed the covers two more rockers have oil. something is not right.
left the valve covers off, turn the drill on, within 5 seconds oil shot out the right side back rocker harder than I pee when i was young. ;D
Is the back cam bearing in wrong.
or wrong lifters
anything to check before putting it back on the engine stand.
next time will just put the intake on it and prime the motor on the engine stand. 8) not in the dragster ready to go  :'( :'( :'( :'(
thanks all

Frontenginedragsters:
 Steve:
Is it a Mark IV / late 60's into the 1970's engine block?
The factory installed front oil galley plugs had a very small hole to bleed off trapped air.
The original hydraulic lifters would tick when the engine was cold.
We don't want the bleeder style plugs in when you build a race engine.
Have you turned over the engine while priming? Spark plugs out, no load on the engine.
You can also call me tomorrow @ 585-288-1499 shop / 585-739-1889 cell.
Sometimes talking is easier than typing.

Matt

hotrod316:
Matt,
thanks for your time today!
springs right on.
sorry i cannot sign the waver   :o
my gut still tills me this dumb ass did something wrong  :-[
so apart she goes again it's just $$$$$$$
will let you know if i should have sign the paper!!
or quit playing Gibbs  (NCIA)  and trusting my gut 8) 8


hotrod316:
Matt,
talked to tech person at  lunati,
he say to take the lifter apart a clean it, (we clean them before putting in them in, but not taking them apart)
did that, there was very small piece of something in there, that fixed the one lifter that pees like a 10 year old.
after cleaning all the lifters (apart) and seeing more on how the oil flows through them,
I can see why it could take sometime to get oil to the front rockers.

I SIGNED THE WAIVER FOR YOU!
 NOW IF IT WILL JUST LIGHT  ON
SUNDAY SUNDAY SUNDAY
AGAIN THANKS FOR YOUR
HERE YOUR WAIVER
STEVE MORGAN

hotrod316:
matt,
we lit the little monster yesterday,
man i miss that smell 8)
ran and sounded great.
ran it for 6 mins between 3000 3500 rpm
at six mins the oil pressure gauge started to bounce 65 down to 40 back 65 very fast
we shut it down,
talk about it, thought what the frat!
pull the filter off and cut it open look good.
drain the oil,
added new filter and 8 and half qts oil, green oil.
old oil looked little milky not bad
relit the it, solid 65psi at idle
started raise the rpm up
2000 rpm gauge when nuts shut if off.
shame i do not drink WHAT we burn ;D
think we grabbed a rod bearing
starting pulling the motor apart
found the lifter that peed like a 10 year old boy
that cam lobe gone  i mean GONE!!! LESS THAT 7 MINUTES RUN TIME  (we time the running time)
there most be something i'm missing in this motor
this is two cam wiped out, both on the same side of the motor
will get to the lower end tomorrow to see if we did grabbed a rod bearing
any more thoughts?
o well, time for a good cigar and a mount dew there go my sugar
as always thanks for your time
ANYBODY GOT ANY THOUGHTS
THANKS STEVE M  :D

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